Quick update:
I have had the truck back for a couple of weeks, and everything is running good. The truck is not what I would call fast, but it runs a lot better than before and it's a lot more fun to drive. It's especially nice to drive on the highway now with the overdrive. The cam was broken in with the stock valve springs and then the new Comp springs were installed. I had to upgrade to a Hughes 2,500rpm torque converter because the engine would not idle in gear. And I had to upgrade to a Holley 750HP because the engine would not stay turned on when idling especially with the a/c on and would also fall flat on it's face on the top end with the old carb and the new engine components. After all the bugs were worked out I had the front and rear tubs redone because I was not satisfied with the way they were before. I will be dropping the truck off at the body shop next Monday.
I had the front side markers shaved while the tubs were getting done and the fender lips were also cut and rolled for even more tire clearance.
Electric fuel pump with braided lines and smoothed fenders painted PPG Victory Red which will be the color of the truck.
Carb/Intake
I had to change my air filter setup due to the new intake/carb. I don't like the way paper air fliters look so I ordered a K&N today, it should be here tomorrow.