Wow what a week. My goal was to take a spin on Sunday and I ended up getting there but what a battle. After giving up on hard lines for the coolant to the air compressor I plumbed it with rubber lines only to find out the head had gotten water in it at one time. It froze and cracked the coolant passage. After tearing the head off the compressor, drilling out the ends of the crack, grooving it out, and TIGing it back up I was ready to try it again.
No more coolant leak but the power steering pump was pegging the 3000psi gauge I put in to check my modified relief. It settled down after working the air out so I tried a couple more bumps over relief... it was still way up and after the second bump spiked the gauge the end cap on the steering box blew apart like a shotgun!
The Hybrid turbo was the easy part...
All in all I got to drive her again Sunday night. Man did it feel good. My B-day wish came true.